Review - Belt/disc Sander

Harbor Freight 4 in. x 36 in. Belt / 6 in. Disc Sander

Central Machinery model #97181

[March 17, 2013]

[March 24, 2013 minor additions]

CREATOR: gd-jpeg v1.0 (using IJG JPEG v62), quality = 90

This is a review of the Harbor Freight model 97181 combination belt/disk sander (here is a link to the Google cached page from about the time I bought it). It's important to note the model number of the unit because Harbor Freight will often come out with new models and reviews different models may not be applicable to the unit you have (or are thinking about buying).

Jumping to the Conclusion

If you are reading this review because you are thinking about purchasing this model, let me start my recommendation: For the $80 (sale price) I paid for it, I think I got my money's worth. I like to fine tune and improve (if possible) any equipment I buy, and I will be doing so with this model. However, I did find this model to be solidly built (for the price), and I think the average buyer could take this home, assemble it, and start using it without modification. There is in fact not much assembly to do (almost none if you go along with my explanations on the rest of this page). I have read other reviews of this unit which say that the motor is underpowered, but I do not think that is true. I would say rather that the motor is barely adequate, but it is in fact adequate. To put it another way, this unit has the smallest possible motor on it that will enable the unit to work.

I would also note that, compared to some reviews I have read of earlier models of this unit, it appears that HF has made some improvements. In particular, earlier reviews complain about plastic levers that break easily - these have been replaced with knobs or bolts. Further, the method by which the adjustable table attaches has been much improved - the table is more stable, and can be relocated more easily. Belt changing is more difficult than it needs to be - not difficult, but time consuming (I made some improvements in this area).

I made some minor modifications to the sander as follows:

  • Belt changing: Replaced the screws holding the backplate to simplify removal
  • Disc sander: Switch to hook and loop system, and shimmed the drive shaft
  • Made protractor scales more readable
  • Left (in my opinion un-needed) some parts off
  • Adjusted belt and tightened all bolts

Looking at the Details

Here's the unit as it comes in the box (additional parts shown below). An 80 grit belt is already installed. I checked the unit for loose screws and found everything tight [on further inspection I found that the bolts holding down the motor needed to be tightened] and solid with one exception: The vertical metal post (seen on the front right corner in the photo) was a bit loose, but it was simple enough to snug it up with a wrench (more about this post later).The base of the unit is stamped steel, and the main frame is cast metal (not cast iron, as it is not attracted by a magnet). All other green painted parts are stamped steel. Overall, the unit feels reasonably solid and sturdy.

Parts

Below are parts supplied with the unit. From left to right:

  • Cast metal (aluminum?) sanding disk, peel-and-stick sandpaper disk, and miter gauge for adjustable tilt-table
  • Aluminum tilt-table
  • Hex wrench and stamped steel wrench
  • Stop plate for sanding belt and cover for sanding disk
  • Rubber foot (shown installed) - four are provided
    • At some point in the future I will probably remove the rubber feet and bolt the sander to a piece of plywood, so I can clamp it to the top of my workbench when I am using it, and then move it to storage when I am done.

The cover for the sanding disk appears to be fitted with some sort of vacuum attachment, although presumably if you wanted to do this you would need some sort of adapter (not supplied). In any case, I will be leaving this piece off, as I think it only gets in the way.

Similarly, I will also be leaving the stop plate for the sanding belt off for two reasons: First, it's just one more thing that has to be removed in order to change belts. Second, if you want to use the tilt-table with the belt, you have to remove it anyway. I'll leave the bolt in, just to fill the hole.

Disk and miter gauge

Tilt-table

Disk cover

Wrenches

Stop plate; disk cover parts

Rubber foot

Support Rod

Below is some detail on the vertical support rod that acts as a position stop when the sanding belt is used in the horizontal mode. As can be seen from the bottom view, the rod is simply screwed into the sheet metal base, and then tightened with a washer/nut from above. Because the rod is screwed into relatively thin sheet metal, this is not a very strong connection (but mostly OK since the force on the rod is all vertical). However, as can be seen from the "top view" below, it's easy for the rod to get tilted slightly, so that it doesn't fully engage the stop tab on the belt section. But, as the final top view shows, it's simple enough to gently bend the post back into proper alignment. I think this could be improved by using a washer/nut on the bottom as well as the top of the base, but I'm not going to bother to do this unless it turns out to be an ongoing problem.

Support rod

Bottom view

Top view - not adjusted

Top view - adjusted

Tilt Table

It appears to me that that the tilt table has been improved from earlier models, in two ways:

First, the mounting mechanism has been changed to make it easier to switch between the belt and the disk, and clamp bolts have been substituted for the earlier plastic levers (which apparently almost always broke). The other adjustment lever for the table angle has also been replaced (with a knob).

Second, the bar which supports the edge of the table nearest the belt (or disc) was only held in place in earlier models by the friction of dimples punched in the metal brackets holding the rod. In my model, there are now two set screws (see photo below) which can be tightened, making for a less wobbly table.

Table - top view

Table - side view

Table - bottom view

Table - Bottom - set screws

Table and stop plate conflict

Table detail - clamp bolt

Table detail - clamp bolt

Table detail - clamp bolt

Rollers

The belt rollers on my unit were adequate, although the molding was far from perfect. Other purchasers of this unit have report problems (and fixes) for bad rollers; look here for a good video which shows how to turn the rollers on a lather. The cited reviewer noted that his belt would not track well, as there was no crown on the drive roller; my unit did not have this problem (see photo below - hard to tell from the photo, but a straight-edge shows a properly crowned center). I do notice a little bit of vibration when running the sander - not enough to worry about now, but if it becomes a problem I may try the roller turning method I cited.

I also noted, differently from the cited review, that the black rod which is part of the belt tightening mechanism has had a fiber sleeve added (presumably to eliminate vibration noise) - it would be simple enough to add this if not already present.

Finally, I note that the paint on the bed under the belt is already wearing off after only a brief period of use. I'm not worried about this - in fact I rather expected it. It's not going to adversely impact function as far as I can tell, but I'll keep an eye on it just to be sure.

Checking for crown.

Damper on belt tightener

Wear on bed.

Belt Changing

In order to change the belt on the sander, you need to remove the back plate. The back plate is held on with 2 screws on the left, 2 screws on the right, and 2 screws below (plus the screw for the stop plate if you opt to use that). That's at least six screws you have to remove (and not lose, along with their washers), just to change a belt. Since I am going to use the sander for wood and metal, and since I will want to use different belts for each, that's more hassle than I want to put up with. As already noted, I'm not using the stop plate, so that's one problem eliminated.

I eliminated the side screws by making two long "knurled bolts" from 1/8" steel rod. I threaded the rod on both ends, lock-tited a knurled nut on one end, and made a round nut to go on the other end; the round nuts were epoxied to the frame on the belt side. In practice I just put the back plate in place, insert the knurled bolts through the existing screw holes, and hand tighten them into the round nuts. To make this a bit easier (as it's a little difficult to thread the end of the rod through the far hole), I made a small "guide washer". The guide washer is basically a thick washer, countersunk on one side to create a "funnel," and epoxied to the inside of the backplate over the screw hole so that it "guides" the end of the rod into the hole. The existing screw holes are big enough that a 1/8" steel rod passes through them easily (no need to drill them out).

I eliminated the two bottom screws my making a short knurled nut to fit the existing screw hole. I epoxied a short length of ball chain to the nut, and fasted the other end to the frame, so I could unscrew the nut without worrying about it getting lost. I was going to make two of these, but I found that just one on the right side was enough.

Now I can change the belt by removing just three screws by hand - no tools required.

[Note: Making these bolts and nuts took the most amount of time of any of the improvements I made. I could have made them using off the shelf parts from the hardware store, like threaded rod, nuts, etc., but I figure since I have a lathe I might as well use it!]

Top: Long" knurled bolt" and round nut

Bottom: Short "knurled nut"

"Guide washer"

Knurled bolt installed

Knurled nut installed

Disc Changing (and a tweak)

As with belt changing, I want to be able to change sanding discs easily, so I switched the disc system from PSA (peel and stick) to H&L (hook and loop). I don't usually mention vendors by name, but it took me quite a bit of searching to find an adapter at a reasonable price, so I'll note that I found it at 2Sand.com. The H&L adapter is just what you might think it is: a disk of velcro type material with an adhesive back which you just stick onto the sanding disc plate. I've found it a bit harder to find solid (no hole) H&L sanding disks without having to buy a pack of 50, but I did find a few locally.

With the H&L system I can easily remove and replace disks, and re-use disks as necessary. A quick test of the system showed that it works well, with the sanding disc held nice and flat, with no sign of loosening.

A final note: When attaching the disc plate to the drive shaft (the plate has a set screw which fastens down onto a flat on the shaft), I noticed that although the plate was held onto the drive shaft well, there was a tiny bit of side to side wobble. I made some quick measurements and found that drive shaft diameter was about 50 thou less than the hole in the plate, so I made a little brass shim to fit around the drive shaft. The shim made the plate tight enough that I had to tap it on gently with a hammer (cushioned by a wood block) - no more wobble.

H&L adapter

H&L sanding disk in place

Brass shim for disc plate

Other Details

The angle markings on the miter gauge and tilt table are very hard to read, as the miter gauge is black on black, and the tilt table scale is just stamped into the metal. So I applied a couple of well known techniques to improve their readability. For the miter gauge, I went over the tops of the raised markings with a sliver paint marker; you can see in the pictures below the miter gauge half completed to show the difference, and the completed miter gauge - I also added a dab of day-glo orange paint to the pointer. For the tilt table scale I painted orange day-glo paint onto the scale (and the pointer) and then scraped it off with a paper index card, leaving the paint only in the stamped in parts; after the paint dried I polished off a bit of paint haze with a paper towel and the job was done. The whole job took only a few minutes, and the improvement in clarity is well worth it. Of course, these scales are not meant for precision work, but for a quick and dirty setting they are useful.

Miter gauge half done

Miter gauge completed

Tilt table scale improved

On the bottom of the belt section (located on the removable cover that enables belt changes) is a dust port. It would be impossible to connect a dust collecter or vacuum to this port in the lowered (horizontal) position without a right angle adapter, though it is easily accessible with the belt in the vertical position. Also not that the dust collector is closed off by a molded in plastic disk with five small holes in it, instead of being fully open. I assume this is to reduce the air flow, perhaps to keep the belt from being pulled against the opening by suction.A few words of warning about using a dust collector or shop vacuum with the dust port, if you are using the sander for both wood and metal: Anything that you sand that could be flammable (wood, plastic, aluminum, etc.) could be ignited from sparks created by sanding metal (yes - aluminum dust can burn). IF you are sanding metal make sure any metal sparks are not going to get near anything that burn.

Here's the nameplate on the motor. As other reviewers have noted, this is not a very powerful motor, but most will concede that it is adequate to the job.

Belt Tightening

Here is the belt and pulleys on the motor (right hand side), and the disc/belt-roller (left hand side). The shape of the belt housing makes it look, from the outside, like there is a larger pulley wheel on the motor side, but the two pulleys are in fact of the same diameter. Presumably a somewhat larger pulley could be put on the motor, though whether this would be a useful modification is not known. Perhaps I'll experiment with this later.I found a lot of slack in the belt, so I decided to tighten it up a bit. The belt tension is adjusted by moving the motor mount, held on by four bolts. In loosening these bolts, I found them to be what I would call "firm but not tight" - this may have allowed the tension to slacken up as the motor operated. In any case, I moved the motor (using a wooden stick as a lever) and tightened all of the motor mount bolts. I'm not sure I really needed to adjust the slack, but it was an easy job and did not take long.