Nicole and I sketch a shape for how the peanut shaped connectors should be cut into.
Nicole and I cut the pieces of the two joints of the inside of the syringes and I cut lexan pieces of the top bar of the V8 Engine.
Nicole and I cut the encasings of the syringes into cylinders, sand them down with a belt sander, and hot glue them together.
The hot glue did not hold well and the cylinders kept breaking apart, so we decided to epoxy them together instead.
Nicole went to work at the internal components of the syringes while I CAD-ed the peanuts. Below is a picture of the both of us getting the parts from the innovation lab.
After we got the 3D printed parts, we attached the internal components with vex bolts and lock nuts. Then we put the added the caps and put the whole assembly together.
After testing the movement of the syringe assembly, we realized the peanuts were too wide. Therefore, we filed the sides down.
Since it was really hard to move the internal and external parts of the syringes, we sprayed silicone spray onto the insides of the encasing and replaced the rubber caps with hot glue.
Before
After
To the right, Nicole is seen using the disk sander to make a wider acute angle for the syringe assembly to connect to and smooth out the cut.
At first, Nicole suggested using paper clips to make the rotating axle. After making a prototype, we realized the paper clips were too flimsy. Then, I tried to CAD and 3D print an axle, but that also turned out to be too flimsy. After that, I went to Tribeca Hardware and bought multiple different rods--some hollow, some aluminum, some bronze, some copper. I bent and tested all of them.
After numerous different failed trials, I bend a hollow bronze rod that successfully spun on the base. However, the notches were a little too large in width and did not hold the syringe assembly well.
Here are some pictures of the CAD we made for the 3D printed parts.