Overview of Status of Analysis, Design, Fabrication, Tests, etc.
The overall design of the wind tunnel has now been finalized. The fabrication process has begun with the wind tunnel acrylic structure components being cut out and all other major components ready for machining. The team is also working on the RTD circuit and Labview temperature controller. The team plans on conducting more tests to ensure uniform temperature distribution on the copper plate.
Accomplishments from Previous Week
Obtained fan
Cut wind tunnel structure components
Obtained plate mount components
Obtained components for RTD circuit
Goals for Next Week (list names after each item). Use specific and measurable objectives.
Assemble wind tunnel (Tian)
Machine insulation (Tian)
Finish RTD circuit (Anthony)
Machine plate mount assembly (Austin)
Design Labview temperature controller (Liz)
Sponsor Comments from Last Meeting and Actions Taken to Address these Comments
Seshadri lent us a rotameter, which he said guarantees uniform flow. We can vary the maximum flow speed by varying area.
Using the rotameter would lead to major design changes and more purchases. We will continue to pursue our current design.
Seshadri suggested 2-3 weeks for testing the actual experiment.
We have adjusted our Gantt chart and schedule.
Fan reaches 5m/s without any pressure drop
Instructor Comments from Last Meeting and Actions Taken to Address these Comments
Dr. T said to calculate the steady-state power, at the set point temperatures with the flow on.
Our pressure drop equates to 1.6” of water, so the pressure drop isn’t trivial.
We’re looking into other fans as well as putting fans in series.
Perform a Solidworks heat transfer simulation with different percentages of flux applied at different areas. See whether uniform temperature is achieved.
Use a thermo-interface for the copper plate to address air gaps.
We’re purchasing a thermal conductive adhesive between the heating pad and the copper plate.
IR image of heat source by itself - heat source for physical test was not uniform
RTD solder melts at 280℃.
We’re not going up to 280℃ specifically, but we need to readdress the temperature range with both Nick and Seshadri.
Risks and Areas of Concern
RTD signal conditioning circuit needs to be trouble-shooted (there is a short in the circuit)
Heating pad heats up very quickly
A new fan may potentially be needed to account for pressure drop due to meshes
Resources or Information Required but not Available
What to use for flow speed of 4-15 m/s for calibration?
Schedule
Finish fabrication of wind tunnel by the end of the week in order to perform experiments the following two weeks
Finish RTD signal conditioning circuit
Purchase components for temperature controller
Budget
$216.25 spent, $1783.75 remaining
Progress on Report and Webpage
First draft of report completed
Webpage multimedia page started