VEX Clawbot
VEX Clawbot
While programming the clawbot, I observed notable inconsistencies in its performance. Initially, both the brain and controller were fully charged, but as I continued my programming efforts, the battery percentage of the brain gradually decreased, resulting in slight variations in the robot's movements during test runs. To address this issue, I ensured the clawbot was fully charged before conducting tests, which successfully yielded the desired outcomes in its performance.